An Underground Haulage Problem Solved - How Tonnage Was Increased 125 Per Cent, Using Existing Equipment

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 3
- File Size:
- 322 KB
- Publication Date:
- Jan 1, 1934
Abstract
HAULAGE was one of the many problems to be solved in the successful handling of the Miami Copper Company's low-grade orebody. The ore extracted had to be increased from 1000 to 18,000 tons per 24 hours over the existing track-age and haulage way. This called for increased speed, longer trains, in¬creased car capacity, and a block signal system so as to maintain a fixed schedule and headway. The motive power in service at the time of this transition consisted of Baldwin-Westinghouse 6-ton trolley locomotives. (See Fig. 3.) These locomotives were purchased to handle twenty inverted-V-bottom side-dump cars of 60 cu. ft. capacity. Dimensions were limited as to height on account of ore chutes, width on account of short radius curves, and length of 12 ft. from bumper to bumper- so that the locomotives could be handled on the man and material hoist which has a cage length of 121/ ft. The limited length made it possible to bring the locomotives to the surface for periodic overhauling and major repairs such as changing wheel tires, gears, and
Citation
APA:
(1934) An Underground Haulage Problem Solved - How Tonnage Was Increased 125 Per Cent, Using Existing EquipmentMLA: An Underground Haulage Problem Solved - How Tonnage Was Increased 125 Per Cent, Using Existing Equipment. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1934.