Coal - Flowsheet Changes for Decreased Moisture of Concord Mine Coal

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 4
- File Size:
- 836 KB
- Publication Date:
- Jan 1, 1969
Abstract
In the coal preparation plant at U.S. Steel Corp.'s Concord mine in Alabama, the product moisture was reduced from about 20% to 9% through the development of a workable flowsheet for dying the clean coal. Some of the high points of the conversion of the Concord washer from vibrating screen dewatering to centrifuge drying are presented in this article. The coal preparation plant at the United States Steel Corp.'s Concord mine near Bessemer, Ala., began operations in June, 1950. The basic cleaning circuit consisted of a Chance cone for cleaning the 2-in. x 3/8-in. fraction and concentrating tables for cleaning the -3/8-in. coal fraction. Dewatering of the final product was accomplished with 35-mesh vibrating screens. However, because Concord coal is very friable with 85% passing 3 mesh and 25% passing 28 mesh (Fig. I), a considerable quantity of fines passed through the dewatering screens. To recover these fines, the dewatering screen effluent was sent to two 70-ft-diam hyd rose para tors from which the underflow returned to the dewatering screens and the overflow went to a 175-ft-diam thickener for water clarification, as illustrated in Fig. 2. As might be expected, there was considerable recirculation of the -35-mesh coal in this system. This degraded the coal and led to higher moistures. It also resulted in a fines bleed-off of plant water and thickener underflow to a fine-coal settling pond. In 1961, vacuum filters were installed to supplement the screens and to recover the fine coal lost in the bleed-off. The above system resulted in a product moisture of about 20%. Further reduction to approximately 11% was accomplished by drainage from railroad cars during transit to the coke plant. Control of the moisture at unloading was poor because of variations in operating levels and railroad car availability, but since the Concord coal constituted a relatively small percentage of the over-all coal mix at the coke plant, its high moisture and fluctuations did not seriously hamper coking operations. Early in 1964, however, the proportion of Concord coal was increased with a resulting increase in the moisture of the total coal mix, and this caused difficulties in the coke plant. The increased participation of Concord coal also brought about a shortage of railroad cars which raised the moisture content to a point where the coal became almost impossible to handle. In an effort to alleviate this problem, U.S. Steel initiated a research program to develop a flowsheet for reducing the moisture to approximately 10% and to determine whether the resulting product would be satisfactory for the coke plant. Under this program, an experimental flowsheet for evaluating both a vibratory centrifuge system and a solid bowl centrifuge system was drawn up as shown in Fig. 3. A horizontal vibratory centrifuge was installed to reduce the moisture in the dewatered coarse coal, and a four-cell, flotation machine was installed to clean the -65-mesh portion of the 3/8-in. x 0 table raw coal feed. Several shortcomings in the above circuits were apparent. For one thing, large quantities of repulping water were required. Furthermore, since about half of the flotation feed was of a size consist that could have been cleaned on the tables, these circuits would result in an unnecessary increase in reagent costs and facilities. Maintenance of the hydro separators and pumps for pumping the underflow to the filters,
Citation
APA:
(1969) Coal - Flowsheet Changes for Decreased Moisture of Concord Mine CoalMLA: Coal - Flowsheet Changes for Decreased Moisture of Concord Mine Coal. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1969.