Copper-Smelting Plant Remodeled For Direct Smelting

The American Institute of Mining, Metallurgical, and Petroleum Engineers
Leonard Larson
Organization:
The American Institute of Mining, Metallurgical, and Petroleum Engineers
Pages:
9
File Size:
328 KB
Publication Date:
Jan 1, 1938

Abstract

DURING several years immediately preceding the adoption of wet-charge smelting at McGill, various necessary conditions affecting this procedure, such as plant rearrangement and the metallurgical nature of the concentrate produced at the concentrator, were fully considered. Wet-charge smelting is not altogether novel to the recently reconstructed smelter at McGill. A number of years prior to this improvement, when flotation methods were initiated at the concentrator, large tonnages of wet and (at that time) sticky flotation concentrate were charged directly into the reverberatory furnaces, because of the difficulty in handling the entire tonnage in the roasters. The plant had excess reverberatory units and this surplus furnace capacity was utilized to smelt raw flotation concentrate. During the years 1927 and 1928, a number of actual operating furnace test runs were made to determine in principle the feasibility of wet-smelting operation. Results were encouraging, and in November 1932 the roasting plant was shut down. For some time thereafter the wet feed was delivered directly to the reverberatory side-charging calcine hoppers already in place. Feeding the wet material through the old calcine hoppers and charge holes into the furnace involved considerable labor, but under the conditions existing at that time it was desirable to continue wet smelting even under the handicap of this laborious procedure. The smelting plant during this period was on a curtailed production basis, operating only about 15 days per month. The alternate starting up and shutting down of the roasting plant presented a difficult problem and charging the wet material directly to the furnace entirely eliminated this difficulty. The roasting plant was never operated thereafter. EARLY PROCEDURE Fig. 1 shows the general layout of the smelting plant before the smelter was remodeled. Under this arrangement, all concentrates and fluxes except converter flux were delivered in cars to wooden storage bins, which paralleled the roaster building. The material to be roasted was dis-
Citation

APA: Leonard Larson  (1938)  Copper-Smelting Plant Remodeled For Direct Smelting

MLA: Leonard Larson Copper-Smelting Plant Remodeled For Direct Smelting. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1938.

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