Fuel-Saving in Steel Making

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 2
- File Size:
- 224 KB
- Publication Date:
- Jan 1, 1929
Abstract
THE No. 6 open-hearth furnace at the plant of the Worth Steel Co., Claymont, Del., is the first to be rebuilt according to the Kuehn system. This as well as the other five furnaces at Claymont, has a nominal capacity of 75 tons, but the actual charge is about 242,000 lb. No hot metal being available, the pig-iron is charged cold. Oil of low grade with an asphalt base is used as fuel. These two items have to be kept in mind when discussing the actual fuel consumption. Careful records have been kept covering a five weeks run and the following is a brief summary of them The time required to heat the furnace preparatory to charging from the time a wood fire was started until charging commenced was 36 hours. This, I understand, is much less than with furnaces of standard design. The draft of the furnace, as shown by a gage in the stack-flue, is 1.25 in. The maximum draft with new checkers on former runs was 1.50 in., this draft gradu¬ally decreasing as the checkers closed up. Both of the first helpers claim the present draft is all they need for the proper working of the furnace, and, as with the Kuehn regenerators the draft remains practically the same from beginning to end of a run, this is satisfactory.
Citation
APA:
(1929) Fuel-Saving in Steel MakingMLA: Fuel-Saving in Steel Making. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1929.