Improving the Energy Efficiency of a Rotary Kiln

The Australasian Institute of Mining and Metallurgy
Organization:
The Australasian Institute of Mining and Metallurgy
Pages:
7
File Size:
255 KB
Publication Date:
Jan 1, 2003

Abstract

The Rotary Kiln at TeKumi was commissioned in February 2002. The process involves burning limestone at 1000 - 11 000¦C to produce a burnt lime (CaO) product. This paper describes the design and installation of a trifoil system to improve the energy efficiency of the kiln. An energy balance showed that 32 per cent of the energy was being lost through the flue gases, compared to 5.8 per cent in shell losses and 2.5 per cent lost as heat in the product. The trifoil proved to be the best way to tap the energy from the flue gases. Drying tests showed that a trifoil improved the drying time of limestone by 37.5 per cent, compared to only 25 per cent for a lifter system. The trifoil system increases the surface area for heat transfer in a Rotary Kiln by 180 per cent. The overal energy efficiency of the Rotary Kiln was improved by 15 per cent, resulting in a 15 per cent increase in production and an 80¦C reduction in flue gas temperature. This has reduced dust build up in the ducting while reducing maintenance costs through a reduced fan speed. The trifoil hub was designed with tooths at the centre to prevent shifting. Each trifoil leg has an anchor block on the down side to prevent downward movement of the trefoil legs.
Citation

APA:  (2003)  Improving the Energy Efficiency of a Rotary Kiln

MLA: Improving the Energy Efficiency of a Rotary Kiln. The Australasian Institute of Mining and Metallurgy, 2003.

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