Institute of Metals Division - System Zirconium-Nitrogen

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 8
- File Size:
- 2347 KB
- Publication Date:
- Jan 1, 1957
Abstract
Iodide zirconium was combined with calculated amounts of nitrided zirconium sponge and arc melted to prepare alloys in the 0 to 6 wt pct N region. Annealing treatments were carried out at 21 temperature levels. Metallographic examination of the heat-treated specimens permitted construction of the binary phase diagram from 0 to 6 pct N. Features of the diagram include the peritectic formation of both a and ß solid solutions. The maximum solubility of nitrogen is 0.8 pct in 8 zirconium and 4.8 pct in a zirconium. An X-ray study of nitrided materials was made in the range 6 to 13 wt pct N region because serious nitrogen losses were experienced when attempts were made to arc melt these high nitrogen alloys. PHASE relationships in the Zr-N system have been determined. Due to the inability to retain nitrogen in nitrogen-rich alloys subjected to arc melting, definitive work was possible only in the range 0 to 6 wt pct (0 to 30 atomic pct) N. Sufficient complementary X-ray work was done to permit construction of the binary phase diagram up to 13.3 wt pct (50 atomic pct) N (ZrN). Small ingots were prepared by arc melting master alloys with enough zirconium to produce an alloy of the desired composition. Following pretreatment, alloys were annealed at temperature levels between 600" and 2020°C. Determination of the phase boundaries was then accomplished by metallographic evaluation of specimens quenched from the various temperatures. Incipient melting techniques were used to corroborate solidus curves, and X-ray diffraction was employed to study the nitrogen-rich region of the a + ZrN phase field. Materials Westinghouse Grade 1 iodide zirconium crystal bar served as the base material for this investigation. The as-received bars were lightly sandblasted, pickled in a 20 pct HN0-5 pct HF aqueous solution, rinsed in water and acetone, and dried. They were rolled to about 1/32 in. strip and acid-pickled, followed by water and then acetone rinses. The material was sheared to approximately 1/4 in. squares, cleaned with acetone, and stored for use. Pure zirconium nitride is not commercially available, according to correspondence with possible suppliers. A literature survey indicated that nitrogen may be introduced into zirconium metal by passing nitrogen or ammonia gas over zirconium at an elevated temperature. After considerable experimentation, a train was devised whereby high quality nitrogen was passed through a series of bubblers to remove the last traces of oxygen, through an H,SO, bubbler and a cold trap to remove moisture, and finally over zirconium within a resistance furnace. Hand-picked Bureau of Mines magnesium-reduced zirconium sponge proved more amenable to nitriding than the crystal bar. The nitrogen used was extra pure gas purchased from Linde Air Products Co. The first two bubblers through which the gas was passed contained a solution suggested by L. F. Fieser" as being ideal for removing the last traces of oxygen from nitrogen. The solution contains 20 g KOH, 2 g sodium-anthraquinone ,9-sulphonate, and 15 g NaHSO, dissolved in 100 ml water. It is blood-red and turns brown when contaminated with oxygen. A saturated lead acetate solution, next in the series of bubblers, removed any H2S which might have formed in the 0, removal stage. An H,SO, bubbler and cold trap removed moisture before the nitrogen was passed over the zirconium. The zirconium was contained in a stainless steel screen within a Vycor or quartz tube in a resistance furnace. Unreacted nitrogen passed out of the system through a mercury bubbler. A nitriding run was performed in the following manner: Zirconium was placed in the screen within the furnace tube. The unit was assembled, suitably clamped off, and evacuated to remove the air and moisture within the tube and that trapped by the zirconium sponge. The unit was flushed with nitrogen and evacuated twice. After nitrogen was allowed to pass over the zirconium for about 30 min, the furnace was turned on; several hours were required to reach temperature. The reaction was allowed to continue at temperature for about 4 hr and the screen was then withdrawn from the hot zone of the furnace by means of a Nichrome or Kanthal rod. The screen and its contents were allowed to cool at the end of the tube and were then removed. At 800°C no more than about 5 pct N could be introduced into the sponge zirconium. This material was designated M-1 (master alloy No. 1) and reserved for the preparation of alloys in the dilute nitrogen region. A second set of experiments was conducted at 1000°C; no more than 7.2 pct N could be introduced into the zirconium at this temperature. Enough material (M-2) of this nitrogen content was prepared to produce a second set of alloys to complement the first and to provide alloys in the 0 to 6 wt pct N range. It was hoped that a diffusion anneal plus a re-nitriding might yield a material of higher nitrogen content. The material containing about 7 pct N was therefore given a homogenization treatment at 1000°C for 6 hr under an argon atmosphere. It was
Citation
APA:
(1957) Institute of Metals Division - System Zirconium-NitrogenMLA: Institute of Metals Division - System Zirconium-Nitrogen. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1957.