Minerals Beneficiation - Converting Gravity-Flotation Plant to All-Flotation

The American Institute of Mining, Metallurgical, and Petroleum Engineers
H. A. Hoffman
Organization:
The American Institute of Mining, Metallurgical, and Petroleum Engineers
Pages:
11
File Size:
766 KB
Publication Date:
Jan 1, 1962

Abstract

Competition from an all-flotation plant, with demonstrated economies and efficiencies, plus a change in smelting contract and introduction of improved cyclones lead to conversion from gravity-flotation. Detailed descriptions are given of equipment installed and procedures used at St. Joseph Lead's Federal mill. Future plans include further quality control by instrumentation in all aspects of the mill operation. Also planned are improvements in materials handling systems. Competitive conditions will continue to dictate improvements and changes in the mill flowsheet. The advent of all-flotation mills in the Lead Belt was introduced by the Indian Creek mill in late 1953. This modern and efficient plant then became a pattern for the other mills in this area to re-evaluate their circuits in an effort to develop flowsheets that would improve operating conditions and metallurgy. The Indian Creek mill demonstrated that all-flotation would require considerably less operating and maintenance labor than the combination of tabling and flotation that was common in the Lead Belt at that time. Two significant changes occurred in recent years to allow all-flotation to be seriously considered in other Lead Belt mills. One was a change in the smelting contract which did not require gravity concentrate. Another was the development of cyclones which provided classification of the flotation feed in a very small space. Since the Federal mill was the largest concentrating plant in the Lead Belt it was felt that the greatest savings could be made by investigating the all-flotation possibilities at this mill. Interest was stimulated by the milling and ore dressing Depts. to determine if this mill would be converted without undue cost, provided the metallurgy could be improved. Accordingly, laboratory tests were initiated to learn what metallurgical benefit could be derived. Numerous tests were run which indicated that grinding to all-flotation would improve the tailing by as much as 0.02 pct Pb. This was quite significant when multiplied by the tonnage of ore treated. Projecting the added cost of power for extra grinding and flotation, and the additional flotation reagents required, plus additional new equipment that would have to be purchased, it would still add up to a considerable saving. The all-flotation mill would reduce man power by some 30 pct, and make a metallurgical improvement. Operating costs could be reduced bv 2$ per ton. The metallurgical improvement would amount to 4$ per ton, for a total of 6$ per ton of ore milled. An estimate of the cost of the conversion was set at $250,000. With the savings as estimated this could be paid off in about two years. On paper it therefore seemed attractive enough to justify a mill test. MILL TESTING One section of the Federal mill was made available for use as a separate test circuit. Cyclones and density controllers were borrowed from the Viburnum and Indian Creek mills. Denver flotation cells were obtained from the Desloge mill that was then shut down. Two 10-cell groups of Fagergren flotation machines, consisting of eight roughers and two cleaners in each bank, were segregated from the remainder of the plant. The 9x12-ft rod mill was continued as a primary grinding mill. The two 6%x12-ft mills on this section were converted from rods to balls, and the speed increased to 22.0 rpm. Cyclones were installed to close the circuit of these ball mills. The ground pulp from each of the ball mills was fed separately to its own bank of flotation cells so that two completely separated test circuits could be run in parallel. This test circuit operated on a three-shift basis from Dec. 22, 1959 to Mar. 21, 1960. The first few weeks were occupied in developing conditions for proper metallurgy and trouble-free operations. Results were rather erratic but as the ore dressing laboratory and the mill operators became more familiar with conditions they were able to obtain expected results, which could be duplicated day after day. The last five weeks of testing indicated the best results and are tabulated in Table I. During the first two weeks a Denver unit cell was used on No. 1 flotation circuit. Even though it recovered almost one half of
Citation

APA: H. A. Hoffman  (1962)  Minerals Beneficiation - Converting Gravity-Flotation Plant to All-Flotation

MLA: H. A. Hoffman Minerals Beneficiation - Converting Gravity-Flotation Plant to All-Flotation. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1962.

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