Part VIII – August 1969 – Papers - Solution Kinetics of a Cast and Wrought High Strength Aluminum Alloy

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 7
- File Size:
- 558 KB
- Publication Date:
- Jan 1, 1970
Abstract
Results are presented of a detailed study on the combined influences of ingot dendrite am spacing and thermomechanical treatments on the structure and solution kinetics of high --purity cast and worked 7075 alloy. Solution kinetics were found to depend sensitively on ingot dendrite am spacing and on details of therrnomechanical processing, including amount of reduction and extent of' solution treatment before reduction. An approximate analysis is given for rate of solution of nonequilibrium second phase in the cast and worked structres; results of the analysis are compared with experiment. MICROSEGREGATION in high strength aluminum alloys manifests itself as "coring" (composition differences within the primary aluminum-rich phase), and as interdendritic second phase. The mechanism of formation of the microsegregation is understood, and approximate prediction of the amount of second phase is possible for simple binary systems.1,2 When alloy elements or impurities are present in amounts less than their solid solubility at solution temperature, any phases forming from these elements are termed "nonequilibrium" and can be dissolved by appropriate solution treatment. The rate at which the nonequilibrium phases are removed depends sensitively on their spacing (dendrite arm spacing in the cast material, or band spacing in wrought material). When alloy elements or impurities are present in amounts in excess of their solubility at the solution temperature, second phase particles form an "equilibrium" second phase that does not dissolve in heat treatment and may, in fact, coarsen in such treatment. Usual commercial, high strength, wrought aluminum alloys contain nonequilibrium second phases that were not fully dissolved during ingot processing. They also contain equilibrium second phases resulting from impurities present in amounts greater than their solubility. As has been shown by Antes, Lipson, and Rosenthal,3 and will be demonstrated further in a subsequent paper by the authors,4 significant improvements in mechanical properties of high strength alloys can be achieved by reduction or elimination of these second phases. Methods of elimination are 1) to employ high purity materials to minimize amounts of equilibrium second phase, and 2) to employ suitable thermomechanical processing techniques to fully eliminate nonequilibrium second phases. Work reported herein comprises a study of selected thermomechani- cal processing treatments, and of their influence on solution kinetics of wrought high purity 7075 alloy. EXPERIMENTAL PROCEDURE Melting and Casting. The bulk of the work reported was performed on a single ingot of high purity 7075 alloy. The ingot was 4 in. by 4 in. by 8 in. high, uni-directionally solidified following a procedure previously described.5 The mold was heated to 1350°F before pouring the melt. The bottom chill was carbon coated stainless steel. Water was circulated through the chill after the melt was poured. The 7075 alloy was prepared from high purity virgin material (aluminum, zinc, magnesium) and from master alloys (Al-50 pct Cu, A1-15 pct Cr, A1-5 pct Ti). Final measured melt composition (wt pct) was: Zn Mg Cu Cr Ti Fe Si Al 5.70 2.28 1.35 0.18 0.15 <0.002 <0.012 bal Melting was done in a silicon carbide crucible; all tools were coated with zircon wash to minimize iron contamination; degassing was by bubbling chlorine through the melt. che-rmomechanical Treatments. Detailed studies were made on material taken from a location approximately 13 in. from the chill and 51/2 in. from the chill (i.e., from 1 in. thick slices taken between 1 and 2 in. from the chill and between 5 and 6 in. from the chill). Solution treatment was done at 860°F in an air-circulating furnace with a "bottom drop" arrangement to achieve minimum delay time between solution treatment and quench. Samples solution treated in this way were 2 in. by 2 in. by 1 in. Temperature of the quench water was approximately 10°C. Mechanical reduction was by cold rolling. Samples 11/2 and 51/2 in. from the chill were treated for 12 and 24 hr, respectively, before cold rolling. Reduction by cold rolling was then 4/1, 16/1, and 35/1. In each case, several intermediate anneals (1/2 hr at 860°F) were used to permit reaching the final thickness without cracking; two such anneals were used for the 4/1 reduction, five for 16/1, and six for 35/1. After working, materials were again solution treated for various lengths of time from 0 to 48 hr and quenched in water. Structural Measurements. Secondary dendrite arm spacings were measured using procedures previously described.' For each measurement reported, five photomicrographs were first made at X75. Measurements were made of dendrite arm spacings in at least 20 different grains (grain structure was equiaxed). Grain size measurements were made by running a number of random traverses across photomicrographs of the samples and obtaining the mean lineal intercept. Measurement of the volume percent of second phase and porosity was done by quantitative metallography. A two-dimensional systematic point count was used
Citation
APA:
(1970) Part VIII – August 1969 – Papers - Solution Kinetics of a Cast and Wrought High Strength Aluminum AlloyMLA: Part VIII – August 1969 – Papers - Solution Kinetics of a Cast and Wrought High Strength Aluminum Alloy. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1970.