Production Engineering - Preventing Corrosion in Gas-condensate Wells (TP 2229, Petr. Tech., July 1947)

The American Institute of Mining, Metallurgical, and Petroleum Engineers
P. L. Menaul P. P. Spafford
Organization:
The American Institute of Mining, Metallurgical, and Petroleum Engineers
Pages:
8
File Size:
554 KB
Publication Date:
Jan 1, 1948

Abstract

This paper discusses the most dangerous form of corrosion encountered in condensate-well oil production, the discovery of the agent causing this corrosion and the remedial chemical treatment proved effective by field use. The injection of ammonium hydroxide, even as little as one quart per day, has proved effective in preventing gas-condensate well corrosion. The injection of "Bone oil" is applied to wells producing brines containing calcium and magnesium salts. Introduction The severe corrosion of equipment in high pressure gas condensate wells has been a problem for several years and numerous papers have been presented on the subject. The term "gas condensate" or "distillate well" is applied to a distinct variety of hydrocarbon producing well, the characteristics of these wells being high bottom-hole (formation) pressures and temperatures and high gas production. These wells usually produce about 40 gal of water per million cubic feet of gas and the gas contains from 0.1 pct to 2 pct carbon dioxide. In the operation of this type of well, the operators soon noted severe internal corrosion of the pipe carrying the production. In some instances the dl tubing has been found to be corroded to perforation in eight months. The high well head pressures of 2500 to 8000 psi makes any weakening of the well equipment by corrosion extremely hazardous. Bursting of the well equipment results in very expensive repair operations and may result in the loss of valuable production, loss of the costly well, or even loss of life. In November 1944, a gas-condensate well in a Gulf Coast field producing from 9500 ft showed a tubing leak. The well was "killed" by filling it with mud through the tubing, and then the tubing was pulled. Corrosion was found to have caused several perforations in the tubing, Fig I. While the mud was being circulated to kill the well, a high pressure jet from the corroded hole in the tubing perforated the casing and damaged the well to the extent that the cost of repairs amounted to $75,000. In November 1944, another gas-con-densate well in a Gulf Coast field producing from 11,400 ft showed tubing failure. This well had been producing an average of 2,500,000 cu ft of gas daily for two years. In the workover of this well, it was found that a hole one inch in diameter had corroded through the tubing and that corrosion had reduced the wall of the tubing to less than half the standard thickness over large areas of the interior of the tubing. It was found that corrosion had also caused two leaks in the casing. After four months spent in an attempted workover failed to make the well safe for further production, the well was plugged and abandoned at a total loss of $300,000,00.
Citation

APA: P. L. Menaul P. P. Spafford  (1948)  Production Engineering - Preventing Corrosion in Gas-condensate Wells (TP 2229, Petr. Tech., July 1947)

MLA: P. L. Menaul P. P. Spafford Production Engineering - Preventing Corrosion in Gas-condensate Wells (TP 2229, Petr. Tech., July 1947). The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1948.

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