RI 8295 Methane Drainage: Experience With Hydraulic Stimulation Through Slotted Casing (329f48c2-5d33-4478-8a07-1515d26a44f3)

The National Institute for Occupational Safety and Health (NIOSH)
Stephen W. Lambert
Organization:
The National Institute for Occupational Safety and Health (NIOSH)
Pages:
19
File Size:
999 KB
Publication Date:
Jan 1, 1978

Abstract

The Bureau of Mines examined the wellbore of a vertical gas drainage well in the Mary Lee coalbed to determine the results of specific completion procedures in coal. A jet-slotting tool was used to cut four vertical slots through the casing about 1 ft below the coalbed. Even though stimulation treatment pressure was excessive, hydraulically induced channels were contained entirely within the target coal zone. Sand-filled, induced channels were horizontal, inclined, and vertical, and were propagated in directions similar to bedding planes, rock joint, and coal cleat directions measured in the mine. Variable gas flow rates, recorded during the productive life of the well, were attributed to chronic downhole pump malfunction and the slotted casing below the production zone.
Citation

APA: Stephen W. Lambert  (1978)  RI 8295 Methane Drainage: Experience With Hydraulic Stimulation Through Slotted Casing (329f48c2-5d33-4478-8a07-1515d26a44f3)

MLA: Stephen W. Lambert RI 8295 Methane Drainage: Experience With Hydraulic Stimulation Through Slotted Casing (329f48c2-5d33-4478-8a07-1515d26a44f3). The National Institute for Occupational Safety and Health (NIOSH), 1978.

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