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In Situ Leaching Wellfield Design At San Manuel
By M. J. Rex, K. L. Wiley, D. S. Ramey
In situ leaching, initiated in 1986 at the San Manuel Mine, was economically developed in 1989. The primary reason for this lag time between startup and viable production was the time required for tec
Jan 1, 1995
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Ejemplos De Esquemas De Flujo De Concentracion Gravimetrica
By Frank L. Bazzanella
Se presenta una breve introducción de la concentración gravimétrica, incluyendo alguna discusión sobre los minerales mas comunes recuperados normalmente. Se mencionan las consideraciones importantes p
Jan 1, 1982
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Impact Of Water Sprays On Scrubber Ventilation Effectiveness
By Travis S. Wellman, Jon C. Volkwein
The Bureau of Mines conducted a study to assess the impact of a directional water spray system on a unique single inlet dust scrubber on a low profile mining machine. Tests were conducted in a full sc
Jan 1, 1989
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Finite Element Method In The Prediction Of Subsidence And Roof Collapse Resulting From Underground Coal Gasification
By Evans U. Jegbefume
A plane strain two-dimensional finite element model employing the method of negative reaction loading has been used to model roof collapse and subsidence resulting from the underground gasification of
Jan 1, 1982
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Reflections on and Considerations for Biotech
By J. A. Brierley, C. L. Brierley
The history, current applications and future of biotechnical developments in the metals' extraction industry are reviewed. Bioleaching of copper minerals continues to be the most significant appl
Jan 1, 1993
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Modeling And Simulation Of Mine Hoisting Operations - Introduction
By Tad S. Golosinsk
Use of computers for hoist evaluation and design dates back to the early 1960's. Mine hoist production calculations, repetitive in nature, were computerized first. More elaborate modeling of hois
Jan 1, 1989
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Optimizing Continuous Miner Scrubbers for Dust Control in High Coal Seams
By K. L. Whitehead, R. A. Jankowski, N. I. Jayaraman
Most continuous miner sections utilizing flooded-bed scrubbers also use blowing face ventilation. Blowing ventilation, however, interferes with dust capture and minimizes scrubber effectiveness. To en
Jan 1, 1992
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Thoughts on Ways to Improve Acid Drainage and Metal Leaching Prediction for Metal Mines
By Y. T. John Kwong
Modified after procedures for assessing acid-generating potential of coal spoils, most acid-base-accounting (ABA) analyses inadequately characterize highly varied metal deposits. Although mineralogy c
Jan 1, 2000
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Operations At The Greenvale Nickel Project Mine And Refinery
By John G. Reid
Geologists, employed by the Australian Company, Metals Exploration Limited, discovered nickel laterite enrichment at Greenvale in 1967. A joint venture was arranged with the Freeport Minerals Comp
Jan 1, 1979
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Fundamental Cost Types - Cost Definitions
[Costs may be classified according to their source and behavior: Scale of aggregation - Total costs - Unit costs Time period for which the costs are charged - Product costs - Period costs
Jan 1, 1999
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Oxidation and wetting behavior of chalcopyrite in the absence and presence of xanthates
By J. Pang, S. Chander
The mechanisms of chalcopyrite oxidation in alkaline solutions have been studied using cyclic voltammetry and impedance spectroscopy techniques. The cyclic voltammetry was used to elucidate oxidation/
Jan 1, 1991
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Heterogeneous Equilibria In Ammonia/Laterite Leaching Systems
By S. W. Asihene, K. Osseo-Asare
The leaching and solution treatment operations used in the ammoniacal treatment of laterites depend on the ability to establish and maintain close stability relations between soluble metal ammine comp
Jan 1, 1979
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Gold Road: Anatomy Of A Turnaround
By Douglas B. Silver
Addwest Minerals' turnaround of the Gold Road Mine in 1996 proves the old adage "mines are made, not found." The underground mine, located in Arizona's San Francisco mining district, was reo
Jan 1, 1997
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Mineral Leaching Of Low-Grade Laterite Ores Using "Bioacids" By Molasses Fungal Metabolism
By P. G. Tzeferis
Factory beet molasses media were used as cheap sources of sucrose for microbial leaching of Greek nickeliferrous laterites using strains of Penicillium and Aspergillus sp. Nickel recoveries of up to 6
Jan 1, 1995
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Sierrita And Morenci Upgrade Their Process Technology
The price of copper has gone into the tank. So has gold. Environmental regulations are more restrictive. Global warming has world leaders and environmental groups seeking international regulations to
Jan 1, 1998
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The Work-Crew Performance Model: A Method For Defining And Building Upon The Expertise Within An Experienced Work Force (ad926623-dd0b-4ffd-9afd-e3ffd1095fbc)
By G. T. Lineberry, W. J. Wiehagen, L. L. Rethi
This paper discusses a practical method for enhancing the performance of mining work crews. The method, described as the Work Crew Performance Model (WCPM), seeks to define performance variability wit
Jan 1, 1996
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Investigation of alternative SAG mill recycle treatment options
By R. I. Pennington, J. L. Vanderbeek
Investigations have been conducted at Chino Mines Co. into the effect that SAG mill recycle material (critical size) exerts on SAG mill throughput and specific energy requirements. Tests were conducte
Jan 1, 1987
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Raman Spectroscopy of Electrochemically Oxidized Pyrite and Optimum Conditions for Sulfur Formation
By F. M. Doyle, Jun Li, Milton E. Wadsworth, E. Peters
The Raman spectroscopic technique was used to study electrochernically oxidized pyrite in-situ. It was found that Raman-active sulfur oxidation products could be detected after a proper potential was
Jan 1, 1993
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Economics of Contract Mining or Should I Use a Contract Miner?
By Donald D. Haas
This presentation will discuss a mine owner's evaluation to utilize a contract miner in the development and production of gold properties. I will address both the quantitative and subjective aspe
Jan 1, 1989
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The mass transport of slurry and solid in a laboratory overflow ball mill
By R. Hogg, L. G. Austin, R. C. Klimpel
Slurry densities and holdup were measured for open circuit grinding tests in a laboratory overflow ball mill of 0.3 m diam by 0.6 m long, by emptying and drying after stoppage of the mill. Contrary to
Jan 1, 1990